| Commit message (Collapse) | Author | Files | Lines |
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expected. Commiting to merge to master - will need more testing before we know if it's a perfect solution.
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has been fired. This should help with the occasional issue where the ISR thread is interrupted and moves back to the primary thread where movements continue.
May need to add another line in adjust() that if interrupted==True then coast the motor (not sure what the ramifications of this would be though: if in the process of going home and thread switches back, it might not get all the way home...)
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keeps coming loose if the speed is changed too quickly, rod will hit base if swinging too near extents (need to cut wood on both sides to allow free swinging.
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